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Drilling optimization using mechanical earth model in an overpressured field in East Java, Indonesia: a case study
Proc. Indon Petrol. Assoc., 35th Ann. Conv.
unpublished
The Lengowangi field, located onshore East Java, Indonesia was discovered in 2006. The main challenges in this area have been the over-pressured Lower Ngrayong and Tuban formations. The first well, L-1, was successfully drilled in 2006 and currently produces up to 10 MMCFD. The second well, L-2, was drilled up-dip in 2008, but could not reach the target because of well control issues related to high pore pressure. Well was TD'd about 2800 ft MD shorter than planned depth. * JOB Pertamina
doi:10.29118/ipa.2182.11.e.071
fatcat:f66bhbea4nhutcgmseuawpluue