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This paper analyses the stability of the Duanjiagou landslide on the Bazhong to Guangan Expressway K134–K135 segment in China. The Duanjiagou landslide took place on 4 November 2015. In order to discover the cause of the landslide, we carried out field geological investigations. The indoor physical property experiments were performed by taking the undisturbed soil sample from the borehole cores. To study the strength of the soil, we carried out a saturation direct shear test and saturationdoi:10.3390/ijgi9010023 fatcat:uwbxqtngqfhlbknxcj75e4hepi